Hi all, New problem. After sitting for quite a while ( COVID, you know ), I started the car and got the dreaded engine knocking. The first time it threw misfire codes ( P0300, P0302, P0303, P0304 ). Seems to be continuing to do it whenever I start it.....but no new codes after clearing them. After poking around a bit, I saw it could potentially be : A low 12V battery. Unlikely,...the 12V battery voltage looks fine. Bad ignition coils. Could be...However, seems odd that I got misfires on multiple coils? Bad plugs. Could be....However, same as #2 above...seems odd that I got misfires on multiple coils? Any ideas on what I should do to tackle this? I threw some Techron in and I'm running the engine to see what that does ( not expecting much ). I may try replacing the plugs/coils first...because it looks pretty straightforward ( well, except for having to remove the wipers and cowling in the cold, etc... ). @Mendel Leisk, @Raytheeagle ...I added you in case you have any further ideas. Thanks!
How's the engine coolant level? Does this have a catch can installed? Looked down the throttle body? Cleaned the MAF sensor?
Coolant levels are just dandy....so doesn't appear to be a leaking head gasket ( thank god ). I removed the MAF sensor and inspected it...looks like it is in mint condition. I did originally rule out an EGR blockage issue because I 'recently' replaced the EGR, cleaned the throttle body, etc...( see previous posts ). However, I need to check it just to make sure. Come to think of it,...'recently' was a couple years ago now....but mileage wise, not all that much. I would certainly hope the EGR wouldn't be fouled again so soon, but who knows! Also, I never did get around to installing a catch can...so maybe that plays into it and is another reason why I want to inspect the EGR, etc... Seems like the point of least resistance is to inspect/change the plugs and possibly swap out the ignition coils...However, I also replaced the plugs a couple years ago when I replaced the EGR, etc...so the plugs 'should' be fine. Just really odd that the car has had absolutely no problems until it was sitting around for an extended period of time. Also note that I did have it connected to a battery minder...so the 12V doesn't appear to be the problem ( and was the first thing I checked ). Bummer this has to happen during a Minnesota winter....haha.
I had a real bad cold start incident in 2018 with our old 2010. I left it at the Oakland Airport for 10 days while I was out of town on business. Came back and it was knocking for a solid 20-30 seconds. This was with a catch can installed too. But no adverse effects thereafter. I'd plan on taking the v out for a spin once in a while. Gotta be someplace to go in flyover country in the dead of winter.
Haha yeah..I do need to take it our more. However, I like driving my wife's Elantra GT lately...it is a fun little hatchback! I'm hoping shoving a buttload of Techron thru the system might help...We'll see.
The problem is "seems to be continuing to do it whenever I start it..." which would lead me to test the head gasket before worse things might happen. A coolant combustion gas tester is pretty easy. Too many of these leaks start out small and very occasional.
Well the more I read about misfires, the more I think I need to rule out the dreaded head gasket issue. Certainly might not be the head gasket but best to rule out the worst case scenario first I guess while I'm trying other things. These 'combustion leak testers' are pretty interesting. I ordered one to try : www.amazon.com/gp/product/B000NPDL76/ Also might try the 'endoscope down the plug hole' trick to check the top of the cylinders. Ordered one of these endoscopes to play with : http://www.amazon.com/gp/product/B07ZH9P8QH Why? I like toys...and I have some amazon gift cards burning a hole in my pocket. I'll report my findings back. It may be a while...I also need to find a day warm enough to work in the garage...or also invest in a garage heater. Hmm that might not be a bad idea come to think of it!
My old man in Pennsylvania has a Kerosene heater he keeps around for when he needs to work in the garage in the winter. Does the trick when the maintenance can't wait.
Update on the knocking. Im stumped....but good news....no more knocking....but it just 'started to work'. Even in the bitter cold, etc....See posts above for review. I'm still going to do some diagnosing when it gets warmer out...but I'll take it at this point. Any theories why the knocking magically stopped? Very odd!
Knocking update #2....still no knocking...it seems to have 'went away'. I'm continuing to monitor coolant levels and such. I'm wondering if it may have been an intermittent fuel line thing...or something of that nature. The car had been garaged for long periods of time over the winter ( hooked up to a batter minder ). After a recent discussion on another thread about 'old gas' and the theory of possible intermittent condensation, etc... I'm wondering if it might have been something related...
Knocking update #3. The knocking started again...very regularly. I noticed it intermittently...but our daughter started driving 'the v' daily after her accident ( see Hi all, new Prius C owner | PriusChat ). Unfortunately, she has also noticed the knocking almost daily. I just dropped her off at the airport and drove it for the first time in a couple weeks. Wow...a lot of knocking...enough to throw misfire codes! I was able to drive it home though. When I got home I checked the coolant level and sure enough...the coolant level was lower than it had been. I then used my combustion leak test kit and sure enough...the fluid turned from dark blue to yellow : So TWO telltale signs of head gasket failure now... Luckily, I 'know a guy' and I'm getting a quote...but I know it ain't gonna be cheap! Geez...can the car issues stop now please? Tagging @Mendel Leisk and @Raytheeagle for the heck of it.
That's unfortunate. But @The Critic has done the job before, so he's the one you want to tag. I've shared a garage and lift with him before. He knows the job as well as some helpful tips . Might help your guy out.
As we see once again, initial head gasket failures are very small and self sealing. Its chronic and really independent of good maintenance.
I did some research on specialist shops in the MN area and ended up calling carspecmn.com. Looks like a great shop...and has been mentioned around here on occasion. Quoted me $2900 for the head gasket work...which also includes a new EGR and EGR cooler. Seems in the ballpark for what I was expecting. I'm close to going with them to do the work. I'd rather not get rid of the car as I've done a ton of work myself on it ( read the rest of this thread to see! haha ).
Yes. Initially the leak is so small the engine has to cool off to allow the coolant to foul the plug. The engine starts and quickly pressurizes and expands sealing the leak. Often the leak does not reappear for weeks. People report the rattle went away after they changed plugs, cleaner egrs, etc only to find out a month later its back. Often the advisors say do all these other things to the point a hydrolock occasionally occurs or white smoke is obvious with coolant drops.
See if he will let you keep the old EGR Cooler. When they are cleaned out, people like me buy them as spares to have for the next EGR system clean-out. Soaking an old cooler in solvent for a few years yields a like new part for next time. They sell for $150 on ebay. I may be beating a dead horse here, but do you have a tool that will let you read the "EGR FLOW INSUFFICIENCY" value from the computer? Techstream of course works, but apps on cell phones (example Torque Pro) can get the same data. Just curious to know if there is a specific value where Head Gasket Failure can be predicted without taking anything apart.
Good idea...but I already have a spare EGR cooler. But yeah...I suppose I could sell it. BTW - I already did an EGR swap not too long ago ( edit - I guess it was in 2018 ) when we purchased the vehicle with 128K on it. ( it has around 168K on it now ) : Hi all, new Prius v owner | Page 3 | PriusChat The EGR cooler was NOT completely clogged at the time...but was somewhat clogged. The EGR swap sure didn't seem to help the head gasket situation!